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volatile_block_buffer_runtime_us

`block_buffer_runtime_us` is mangled in the planner and in the stepper-ISR.
So it needs to be volatile and interrupt protected.
pull/1/head
AnHardt 8 years ago
parent
commit
13eebd11cf
  1. 6
      Marlin/planner.cpp
  2. 21
      Marlin/planner.h

6
Marlin/planner.cpp

@ -146,7 +146,7 @@ float Planner::previous_speed[NUM_AXIS],
#endif
#if ENABLED(ENSURE_SMOOTH_MOVES)
uint32_t Planner::block_buffer_runtime_us = 0;
volatile uint32_t Planner::block_buffer_runtime_us = 0;
#endif
/**
@ -1007,7 +1007,9 @@ void Planner::_buffer_line(const float &a, const float &b, const float &c, const
segment_time = (MIN_BLOCK_TIME) * 1000UL;
}
block->segment_time = segment_time;
block_buffer_runtime_us += segment_time;
CRITICAL_SECTION_START
block_buffer_runtime_us += segment_time;
CRITICAL_SECTION_END
#endif
block->nominal_speed = block->millimeters * inverse_mm_s; // (mm/sec) Always > 0

21
Marlin/planner.h

@ -215,7 +215,7 @@ class Planner {
#endif
#if ENABLED(ENSURE_SMOOTH_MOVES)
static uint32_t block_buffer_runtime_us; //Theoretical block buffer runtime in µs
volatile static uint32_t block_buffer_runtime_us; //Theoretical block buffer runtime in µs
#endif
public:
@ -387,21 +387,26 @@ class Planner {
SBI(block->flag, BLOCK_BIT_BUSY);
return block;
}
else
else {
#if ENABLED(ENSURE_SMOOTH_MOVES)
clear_block_buffer_runtime(); // paranoia. Buffer is empty now - so reset accumulated time to zero.
#endif
return NULL;
}
}
#if ENABLED(ENSURE_SMOOTH_MOVES)
static bool long_move() {
if (block_buffer_runtime_us) {
return block_buffer_runtime_us > (LCD_UPDATE_THRESHOLD) * 1000UL + (MIN_BLOCK_TIME) * 3000UL;
}
else
return true;
CRITICAL_SECTION_START
uint32_t bbru = block_buffer_runtime_us;
CRITICAL_SECTION_END
return !bbru || bbru > (LCD_UPDATE_THRESHOLD) * 1000UL + (MIN_BLOCK_TIME) * 3000UL;
}
static void clear_block_buffer_runtime(){
block_buffer_runtime_us = 0;
CRITICAL_SECTION_START
block_buffer_runtime_us = 0;
CRITICAL_SECTION_END
}
#endif

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